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Case Studies

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Late-Life ≠ High Risk

Reframing redundant well management against operational baseline, not zero-risk expectations.

Late-Life ≠ High Risk

Rethinking SCSSV Testing

US$15M saved annually through smarter testing.

Rethinking SCSSV Testing

~500 MMscf/d, Zero Incidents

Independent technical authority across a three-well offshore commissioning campaign.

~500 MMscf/d, Zero Incidents

One Standard. Ten Assets. Three Continents.

Eliminating inconsistent ICV practices across a global portfolio with two definitive technical guides.

One Standard. Ten Assets. Three Continents.

Barrier Audit

Result MCGx delivered a consolidated barrier audit covering more than 500 LOT and FT signatures from over 40 wells, giving...

Barrier Audit

Leak Found. Production Held.

Targeted remediation that avoided a blind subsea campaign and preserved field economics.

Leak Found. Production Held.

100+ Operators, US$4B at Stake

Converting fragmented engineering documentation into a training narrative operators could actually use.

100+ Operators, US$4B at Stake

Two Wells, Two Hidden Threats

Detecting an inadvertently closed ICV and a sand-detector spike before they took 490 MMscf/d offline.

Two Wells, Two Hidden Threats

US$90M Avoided. US$100k Spent.

A passive ICV solution that turned a planned subsea intervention into a US$100k fix with zero downtime.

US$90M Avoided. US$100k Spent.